MWC UNIT # |
POLLUTANT OR PARAMETER |
START DATE mm/dd/yyyy |
START |
FINISH |
MONITORED LEVEL |
APPLICABLE LIMIT |
SPECIFIC REASON FOR EXCESS |
CORRECTIVE ACTIONS TAKEN |
| |
|
|
|
|
|
|
|
|
| 1 |
CO |
1/28/2002 |
2000 |
2400 |
312 |
69 |
shutdown |
followed shutdown procedures |
| 1 |
CO |
2/3/2002 |
0800 |
1200 |
559 |
69 |
shutdown |
followed shutdown procedures |
| 2 |
CO |
3/7/2002 |
0000 |
0400 |
469 |
69 |
turbing tripped-malfunction of lube oil system, back up system failed ti maintain pressure switch |
initiated emergency response procedures to reduce steam load, secure and stablize units and plant. |
| 1 |
CO |
3/7/2002 |
0000 |
0400 |
293 |
69 |
turbing tripped-malfunction of lube oil system, back up system failed ti maintain pressure switch |
initiated emergency response procedures to reduce steam load, secure and stablize units and plant. |
| 2 |
CO |
3/20/2002 |
1200 |
1600 |
219 |
69 |
shutdown due to tube leak |
followed shutdown procedures |
| 2 |
CO |
3/21/2002 |
2000 |
2400 |
273 |
69 |
shutdown due to tube leak |
followed shutdown procedures |
| 2 |
CO |
4/19/2002 |
1600 |
2000 |
84 |
69 |
shutdown due to tube leak |
followed shutdown procedures |
| 1 |
CO |
4/29/2002 |
0400 |
0800 |
457 |
69 |
shutdown due to tube leak |
followed shutdown procedures |
| 2 |
CO |
5/12/2002 |
0000 |
0400 |
237 |
69 |
shutdown due to tube leak |
followed shutdown procedures |
| 1 |
CO |
5/15/2002 |
1200 |
1600 |
187 |
69 |
planned shutdown |
followed shutdown procedures |
| 2 |
CO |
5/17/2002 |
2000 |
2400 |
135 |
69 |
planned shutdown |
followed shutdown procedures |
| 2 |
CO |
5/19/2002 |
0800 |
1200 |
365 |
69 |
while returning facility to operation a tube leak developed which required unit to be shutdown for repairs |
followed shutdown procedures |
| 1 |
CO |
6/26/2002 |
1600 |
2000 |
97 |
69 |
fire at substation knocked turbine off line and analyzers |
initiated emergency response procedures to reduce steam load, secure and stablize units and plant. |
| 2 |
CO |
6/26/2002 |
1600 |
2000 |
537 |
69 |
fire at substation knocked turbine off line and analyzers |
initiated emergency response procedures to reduce steam load, secure and stablize units and plant. |
| 2 |
CO |
6/27/2002 |
0000 |
0400 |
211 |
69 |
start-up of plant delayed |
had to reset Turbine control limits to 2 boiler operation status |